Analysis and optimization of CHP plant Plock
Conducting energy audit at CHP plant in Plock refinery and recommendation of appropriate measures for achieving energy savings.
Services provided:
- Energy audit at CHP plant in Plock refinery
- Collecting relevant technical data
- Conducting thermodynamic and hydrodynamic process calculations of CHP plant
- Identification of appropriate measures for achieving energy savings
- Preparation and elaboration of a report with technical and economic aspects of selected measures for achieving energy savings
Key data:
- Seven conventional steam boilers (170-290MW)
- Fresh steam pressure: 137 bar
- Fresh steam temperature: 550°C
- Six back-pressure steam turbines, rated power 55MW
- One condensing steam turbine, rated power 70MW
- Seven steam collectors
- Two steam stations
- Steam distribution network length 240km
Time period: 2012